Technical Session 39: Stimulation and Conformance for Sustainable Production Delivery
Thursday, 20 February
Room 406-407
Technical Session
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1100-1130 24732Monetizing Value Of Early Gas Cap Blowdown (GCBD)
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1130-1200 24808Well Trajectory Optimization Has Been Successful In Delivering 1000 Bopd By Revisiting Seismic Anisotropy Pre-stack Depth Migration (PSDM) To Minimize Structural Uncertainty. Case Study: Infill Well Bmax-12st Brown Field, Pertamina Offshore Northwest Java
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1200-1230 24863Pushing Injectivity Limits Via Waterflooding In Fractured Injection Conditions - An Automated Approach To Make It Safe, Manageable And Sustainable
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Alternate 24778Maximizing Value In Mature Waterflood Field
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Alternate 24953Geosteering In Laminated Porcellanitic Barmer Hill Formation: A Case Study From Tight Oil Development Reservoir, India
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Alternate 24809Chasing Remaining Thin Oil Column In Mature Gas Injection Reservoir With Active Aquifer
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Alternate 24671Enhancing Value From A Matured Offshore Field: Optimal Infill Campaign Leveraging Subsurface Insights And Analytical Reservoir Engineering
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Alternate 24949Optimizing Well Placement In Unconsolidated Reservoir Using High-definition Reservoir Mapping And Rotary Steerable System: A Case Study In The South China Sea